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Gary Brown
2025-06-21T16:31:00 permalink Post: 11907891 |
Some assumed numbers about normal biotreatment.
https://www.biobor.com/wp-content/up...ation-IATA.pdf If we assume 50 tonnes fuel load a 100ppmw biotreatment will be 5kg of biocide total in all tanks. The GEnx-1B will burn about 4,5kg/s fuel each on a take off run (give or take a bit) so 9kg/s in both donks for about 20s until rotate. So the total nominal biocide dose could be pumped in about half a second through both engines on take off power if it where not mixed at all and arrives in both engines at the same time. This gives you an idea that with the nominal amount of biocide dose not much could have happened. If biocide is the source of this dual EFATO than an extreme overdose in addition to wrong application preventing mixture with the fuel had to be the case. Neither incident reports make for pretty reading. But, in neither case did they experience near-simultaneous engine failure (not far off that, but still assymetric). Last edited by Gary Brown; 22nd Jun 2025 at 08:19 . Reason: Correcting math error from 100 x to 10 x ... 3 users liked this post. |
JPI33600
2025-06-21T17:23:00 permalink Post: 11907918 |
(5) From the results of the interview with the CS who was in charge of biocide treatment work, it is probably that the CS calculated according to the AMM so that the recommended final concentration ratio in the tanks would be about 100 ppm, and additionally loaded the treated fuel as described in 2.7 (11).
According to the AMM calculation formula, the concentration ratio of the additional biocide treated fuel is calculated to be about 250 ppm in the left tank and about 285 ppm in the right tank. However, there was no record of the calculation of the concentration ratio of the biocide and the dosage amount. It is desirable to keep these records because they are considered to be important for traceability of maintenance work. 2 users liked this post. |
GroundedSpanner
2025-06-22T00:15:00 permalink Post: 11908173 |
I don't want to refute your theory, but given your 30 years of experience---presuming it is relevant--I'd ask you to clarify a few things.
First, water in fuel is not a novel concept and I would presume that the designers of the 787 knew about it. You've simply stated that water might collect and settle out, but how much water might you expect under those conditions (57% humidity doesn't seem terribly high to me) and what features and procedures are already there to mitigage water contamination issues? Your theory would imply that there basically aren't any. IDK how the tank venting system works, but the idea that some huge amount of water could have condensed in the tank from the outside seems preposterous. Second, how much water do you think it would take to cause a sustained flameout in one of those engines? Remember that they have automatic continous relight, so you're going to have to sustain your flame suppression long enough for them to wind down completely. I think those engines were probably using something like 2 gallons per second of fuel along with 250lbs of air heated to over 1100F. Any fuel in the mix would burn and the water would be converted to steam so you'd need mostly water for a long time. So if you think a hundred gallons of water could have gotten into each tank then perhaps I'd buy your theory--which, btw, does fit the known facts pretty well. But I think that short of some woeful neglect, Boeing and AI already know about and have methods of dealing with water contamination. At least I hope so. Experience. Without wishing to dox myself, I've worked in engineering at a major airline from apprentice through (in no particular order) Line Maintenance, Heavy and Light Maintenance, to technical support and maintenance control on both Boeing and Airbus products, with various qualifications and authorisations along the way. [Hmm - Scrap this sentence?]On the day 9/11 occurred, I should have been making modifications inside a fuel tank instead of staring at the TV with mouth on the floor. However, I would describe my experience as broad, yet shallow in respect to this incident. Some of my fleet I know every rivet. Some of my fleet I've only ever seen from a distance. I don't touch airplanes for a living any more. B787 though - is not my area of specialty. I'll dig in, but am not the expert. I am not a systems design engineer, so precise numbers and flow rates, are not what I do. But what the systems do, how they operate, what they look like, smell and taste like... yeah, I'm not a muggle. And I do have access to all the manuals and know how to use them. And - let me be clear, I am speculating. I was advancing a theory. It WILL be some flavour of wrong. The investigation will reveal all. I Agree, Water in fuel is not a novel concept. Aircraft fuel tanks attract water - fact. How much? It varies. I've sumped tanks and got no water, I've seen drops of water beading about in the bottom of a gallon jug, I've seen gallons of water. I've been so covered in fuel I cant smell it or think straight and taken gallon after gallon not being able to tell if its fuel or water. I also agree that 57% humidity doesn't seem particularly high - its not south east Asian jungle levels - but I'm not an expert at humidity, 32Deg c at 57% humidity at 02:30 am is not going to be comfortable for me though. I looked at recent weather in DEL, and those values were at the higher end of the range. Further, I believe the prevailing weather conditions on the ground are less important when it comes to the volume of water getting in. Fuel is cold, or gets damn cold during a 9 Hr flight. Fuel Temperature Management is an issue for our Drivers. So as the fuel is used at altitude, Air enters the tank through NACA Ducts in the outboard end of the wing. Its beneficial to maintain a slight positive pressure, amongst other things to reduce evaporation. (Added complication, there is also the Nitrogen Enrichment system due to TWA800 - but that's more about processing the air in the tank to change the properties and make it non-explosive). Then as the aircraft descends, more air enters as the air pressure increases. Its the humidity of that air in the descent that is going to determine the volume of water entering the tank and potentially the fuel. The water in the air condenses on the sides of the tank because of the cold post-flight fuel. It doesn't dissolve into the fuel, but sinks to the bottom. Ground temperature / humidity and time will likely affect how much water condenses out of that air while on the ground. There won't be a huge amount of air exchange on the ground. Likely if the AC landed at 2am, then from sunrise as the tank warmed up, there would actually be a flow out of the vents. What Features and procedures are there to mitigate Water? I apologise if my post gave the impression that there are no mitigation processes. There are. Water is well understood in the industry. Well for a start, Features / Design. The Aircraft has a water scavenge system. Water doesn't mix with fuel, it sinks to the bottom being about 20% denser than fuel, so at the very lowest point in the tank, the water scavenge system (Powered by the Aft Fuel Pump through a jet pump, a venturi like system) will suck up the 'fluid' at the very lowest point, where the water would collect and in Boeings words 'drip' that fluid into the path of the pump pickup inlet (but I'd describe it more as a 'squirt'). The idea being that a small amount of water injected into the fuel will be consumed by the engines harmlessly. There is also agitation. The wing tank pumps are pretty much running constantly, from before engine startup to after engine shutdown. The pumps are quite violent to the fuel and supply more pressure then the engine could ever need. Any excess pressure is dumped right back into the tank, quite close to the pump, in a direction that would further stir up the fuel and help break up any water into suspended droplets. This all works if there is a small amount of water in the fuel. The water scavenge pickup is right next to the pump inlet, but a bit lower. Little bits of water get managed. Looking at the pictures of the system, I'd say a couple of gallons of water would do no harm at all. But if there was significantly more water in that tank. Guessing 10-30 + gallons, then the pump would be circulating water, or highly water rich fuel. Then there's the suction pickup. Its in the same 'bay' as the aft fuel pump and located a little 'higher' than the pump inlet and water scavenge inlet. But also located between stringers that can separate out the settled water ( I wish I could share the pictures, but more than my job is worth ) I can imagine the suction pickup being in a pool of 'stagnant' water. I also saw a post from Metcha about the scavenge system blocking with Algae - I don't know about that (B787 not my fleet). But possible that could aggravate things. There's also the reports of the Indian AAIB looking at the Titan Biocide incident. Its possible that might be related and could modify the theory. Procedures - There's the (at my airline weekly I think) procedure to 'sump' the tanks. There are drain points in the tank. Valves that you can push in with a tool and fluid drains. As described earlier (and videos exist on YouTube), you drain about a gallon of fluid and examine it for water. Most often in temperate climates (my experience), there's a few 'beads' of water in the bottom of the jug, moving about like mercury. Except when there's more. Sometimes there's a clear line in the jug, half water, fuel above. And sometimes a gallon of water, that smells like fuel. You drain it until you are sure there's no water. Could 'that much' water have condensed in the tank? Well - There's the question. I guess the basis of the theory is that on descent into DEL, the wing tanks picked up some very humid air, which settled water into the tanks through the night. Then, as the theory I posited must work, the wing pumps must have circulated and suspended that water into the fuel. By design, the water from the CDG-DEL arrival should have been consumed in the DEL-AMD Sector. But desperately clinging to defending my theory (I appreciate this is a hole), lets assume that at DEL the pumps were running for a long time. Lets assume that the pumps allowed the water to be dispersed within the tank prior to being used through the engines. Then - in the DEL-AMD sector, the wing tanks could have picked up more water. How much water would cause a sustained flameout? I never posited a sustained flameout. I posited a significant reduction in thrust. Listening back to the rooftop video, which at first we were all listening for evidence of RAT, there's also a rhythmic pop-pop-pop of engines struggling. I think the engines were running, albeit badly. Heavily water contaminated fuel will do that. It doesn't have to be 100% water. Just enough water to make the engine lose thrust. Your 2 gallons per second figure assumes the engine running at full flow. I'm not a figures man, I'll not challenge that, I do recall flowmeters at max thrust spin like crazy. But an engine struggling due to a high perrcentage of contamination, is that using 2 gal/sec? or just trying to? What happens if there is e.g. 20% water in the fuel? There are also reported incidents of engine flameout / thrust reduction that have all happened at altitude. Incidents that have been recovered due to the altitude and time available. I Posited that the engines would have eventually regained full thrust once the contamination worked though. But 30 seconds of rough engine is very different at 40,000 feet than it is at 100 feet. The theory also relies on a second part - the electrical failure. That the electrical failure causes the fuel supply to switch, a few seconds after the failure. We go, at the point of electrical failure from a pumped centre tank supply to a sucked wing tank supply. It takes time for that different fuel to reach the engine. Ive written enough and am tired. Must stop now. 11 users liked this post. |
Gary Brown
2025-06-22T08:15:00 permalink Post: 11908347 |
For the Gatwick indident, read p2 of the AAIB Final Report for the figure of 38 x correct dosage. The rest of the report will tell you how AAIB arrived at that figure (mostly, though not entirely, by testing the fuel post landing...).
I'll double check my claim of 100 x for the Japan incident tomorrow. I'm on cooking duty this evening..... The difficulty in ascertaining the over-dosage in all these instances is that a) there was no general requirement to keep a record of the concentration calculated and used, and b) in each case the biocide admixture was done several days, several flight cycles, and several re-fuellings before the incident, and in most cases at a maintenance facility a long way from the incident route. 2 users liked this post. |
GroundedSpanner
2025-06-30T22:21:00 permalink Post: 11913922 |
OK - Fair Challenges - good post, I'll have a go at answering and simultaneously expanding my own thoughts. In fact I'm not having a go at you, I'm more working my theory....
Experience. Without wishing to dox myself, I've worked in engineering at a major airline from apprentice through (in no particular order) Line Maintenance, Heavy and Light Maintenance, to technical support and maintenance control on both Boeing and Airbus products, with various qualifications and authorisations along the way. [Hmm - Scrap this sentence?]On the day 9/11 occurred, I should have been making modifications inside a fuel tank instead of staring at the TV with mouth on the floor. However, I would describe my experience as broad, yet shallow in respect to this incident. Some of my fleet I know every rivet. Some of my fleet I've only ever seen from a distance. I don't touch airplanes for a living any more. B787 though - is not my area of specialty. I'll dig in, but am not the expert. I am not a systems design engineer, so precise numbers and flow rates, are not what I do. But what the systems do, how they operate, what they look like, smell and taste like... yeah, I'm not a muggle. And I do have access to all the manuals and know how to use them. And - let me be clear, I am speculating. I was advancing a theory. It WILL be some flavour of wrong. The investigation will reveal all. I Agree, Water in fuel is not a novel concept. Aircraft fuel tanks attract water - fact. How much? It varies. I've sumped tanks and got no water, I've seen drops of water beading about in the bottom of a gallon jug, I've seen gallons of water. I've been so covered in fuel I cant smell it or think straight and taken gallon after gallon not being able to tell if its fuel or water. I also agree that 57% humidity doesn't seem particularly high - its not south east Asian jungle levels - but I'm not an expert at humidity, 32Deg c at 57% humidity at 02:30 am is not going to be comfortable for me though. I looked at recent weather in DEL, and those values were at the higher end of the range. Further, I believe the prevailing weather conditions on the ground are less important when it comes to the volume of water getting in. Fuel is cold, or gets damn cold during a 9 Hr flight. Fuel Temperature Management is an issue for our Drivers. So as the fuel is used at altitude, Air enters the tank through NACA Ducts in the outboard end of the wing. Its beneficial to maintain a slight positive pressure, amongst other things to reduce evaporation. (Added complication, there is also the Nitrogen Enrichment system due to TWA800 - but that's more about processing the air in the tank to change the properties and make it non-explosive). Then as the aircraft descends, more air enters as the air pressure increases. Its the humidity of that air in the descent that is going to determine the volume of water entering the tank and potentially the fuel. The water in the air condenses on the sides of the tank because of the cold post-flight fuel. It doesn't dissolve into the fuel, but sinks to the bottom. Ground temperature / humidity and time will likely affect how much water condenses out of that air while on the ground. There won't be a huge amount of air exchange on the ground. Likely if the AC landed at 2am, then from sunrise as the tank warmed up, there would actually be a flow out of the vents. What Features and procedures are there to mitigate Water? I apologise if my post gave the impression that there are no mitigation processes. There are. Water is well understood in the industry. Well for a start, Features / Design. The Aircraft has a water scavenge system. Water doesn't mix with fuel, it sinks to the bottom being about 20% denser than fuel, so at the very lowest point in the tank, the water scavenge system (Powered by the Aft Fuel Pump through a jet pump, a venturi like system) will suck up the 'fluid' at the very lowest point, where the water would collect and in Boeings words 'drip' that fluid into the path of the pump pickup inlet (but I'd describe it more as a 'squirt'). The idea being that a small amount of water injected into the fuel will be consumed by the engines harmlessly. There is also agitation. The wing tank pumps are pretty much running constantly, from before engine startup to after engine shutdown. The pumps are quite violent to the fuel and supply more pressure then the engine could ever need. Any excess pressure is dumped right back into the tank, quite close to the pump, in a direction that would further stir up the fuel and help break up any water into suspended droplets. This all works if there is a small amount of water in the fuel. The water scavenge pickup is right next to the pump inlet, but a bit lower. Little bits of water get managed. Looking at the pictures of the system, I'd say a couple of gallons of water would do no harm at all. But if there was significantly more water in that tank. Guessing 10-30 + gallons, then the pump would be circulating water, or highly water rich fuel. Then there's the suction pickup. Its in the same 'bay' as the aft fuel pump and located a little 'higher' than the pump inlet and water scavenge inlet. But also located between stringers that can separate out the settled water ( I wish I could share the pictures, but more than my job is worth ) I can imagine the suction pickup being in a pool of 'stagnant' water. I also saw a post from Metcha about the scavenge system blocking with Algae - I don't know about that (B787 not my fleet). But possible that could aggravate things. There's also the reports of the Indian AAIB looking at the Titan Biocide incident. Its possible that might be related and could modify the theory. Procedures - There's the (at my airline weekly I think) procedure to 'sump' the tanks. There are drain points in the tank. Valves that you can push in with a tool and fluid drains. As described earlier (and videos exist on YouTube), you drain about a gallon of fluid and examine it for water. Most often in temperate climates (my experience), there's a few 'beads' of water in the bottom of the jug, moving about like mercury. Except when there's more. Sometimes there's a clear line in the jug, half water, fuel above. And sometimes a gallon of water, that smells like fuel. You drain it until you are sure there's no water. Could 'that much' water have condensed in the tank? Well - There's the question. I guess the basis of the theory is that on descent into DEL, the wing tanks picked up some very humid air, which settled water into the tanks through the night. Then, as the theory I posited must work, the wing pumps must have circulated and suspended that water into the fuel. By design, the water from the CDG-DEL arrival should have been consumed in the DEL-AMD Sector. But desperately clinging to defending my theory (I appreciate this is a hole), lets assume that at DEL the pumps were running for a long time. Lets assume that the pumps allowed the water to be dispersed within the tank prior to being used through the engines. Then - in the DEL-AMD sector, the wing tanks could have picked up more water. How much water would cause a sustained flameout? I never posited a sustained flameout. I posited a significant reduction in thrust. Listening back to the rooftop video, which at first we were all listening for evidence of RAT, there's also a rhythmic pop-pop-pop of engines struggling. I think the engines were running, albeit badly. Heavily water contaminated fuel will do that. It doesn't have to be 100% water. Just enough water to make the engine lose thrust. Your 2 gallons per second figure assumes the engine running at full flow. I'm not a figures man, I'll not challenge that, I do recall flowmeters at max thrust spin like crazy. But an engine struggling due to a high perrcentage of contamination, is that using 2 gal/sec? or just trying to? What happens if there is e.g. 20% water in the fuel? There are also reported incidents of engine flameout / thrust reduction that have all happened at altitude. Incidents that have been recovered due to the altitude and time available. I Posited that the engines would have eventually regained full thrust once the contamination worked though. But 30 seconds of rough engine is very different at 40,000 feet than it is at 100 feet. The theory also relies on a second part - the electrical failure. That the electrical failure causes the fuel supply to switch, a few seconds after the failure. We go, at the point of electrical failure from a pumped centre tank supply to a sucked wing tank supply. It takes time for that different fuel to reach the engine. Ive written enough and am tired. Must stop now. Last edited by Senior Pilot; 30th Jun 2025 at 23:01 . Reason: Quote from a week ago; this is not a Hamsterwheel thread, thanks! |