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Sisiphos
2025-06-14T06:53:00 permalink Post: 11901175 |
Speaking as a B787 Captain..... There is so much rubbish and stupid suggestion being written here.
This aircraft was airborne for a grand total of 22 seconds, half of which was climbing to no more than 150' aal. - No Flaps? Due to the setup of the ECL it is physically impossible to go down the runway without some sort of take-off flap set. The T/o config warning would have been singing it's head off. Despite assertions to the contrary I have seen no video clear enough to detect a lack of flaps. - RAT out? Almost impossible, I have seen no quality footage that definitively witnesses the RAT being out. Those who think they car hear a RAT type noise might be listening to a motorcycle passing or similar. It takes a triple hydraulic failure or a double engine failure to trigger RAT deploment. They happily went through V1 without a hint of rejected take off so as they rotated the aircraft was serviceable. These are big engines, they take a long time to wind down when you shut them down. I have never tried it however engine failure detection takes 30s or for the aircraft to react and they were not even airborne that long. - Flaps up instead of gear? The B787 flaps are slow both in and out. Given that the 'Positive rate' call is not made the second the wheels leave the ground, a mis-selection of flaps up would not cause any loss of lift for at least 20 seconds, by which time they had already crashed. I believe the gear remained down not because of mis-selection but because of a major distraction on rotate. Discounting the impossible, two hypotheses remain: 1. Invalid derate set through incorrect cross-checking. Trundling down the runway takes very little power to reach Vr. It is only when you rotate that you create more drag and discover that you do not have sufficient thrust vs. drag to sustain a climb. Or.... 2. Put 200' as the altitude target in the FCU. Immediate ALT capture and all the power comes off. PF is still hand flying trying to increase pitch but is already way behind the aircraft. It could be after this that Boeing are forced to review the B787 practice of exploring the very edges of the performance envelope. 1) The flap retraction would immediately result in progressive less lift, not only after full retraction . The time in the air could have been longer than your estimate, maybe enough time for full retraction 2) if 200 feet in MCP, why would that lead to a descent? Shouldn't that result in level flight? 3) wrong TOW / too low power setting sounds like a plausible event.Happened before. But with full power / TOGA set in the air ( which surely must have happened)I would expect at least a longer struggle rather than the constant descent. Just a gut feeling though, busdriver, no experience on 787. Maybe already in a power on stall. The only problem with this hypothesis is that it does not explain the gear down since there definitely was positive rate after rotation. 4) double engine failure too remote, no signs of flames etc. Forget it, agreed. My guess remains inadvertant flaps retraction for what it's worth. 1 user liked this post. |
Someone Somewhere
2025-06-14T07:22:00 permalink Post: 11901193 |
![]() (I screwed up earlier and had a 767 image here...)
Taken together, it seems that there was an event (or events) shortly after rotation that compromised both engines and the electrical system.
Compromising both engines inherently compromises the electrical system: dropping below idle N2 (plus some safety margin) disconnects generators. Last edited by Someone Somewhere; 14th Jun 2025 at 17:57 . 2 users liked this post. |
Greenlights
2025-06-14T07:27:00 permalink Post: 11901197 |
hello guys,
I'm pilot but not on a heavy one, so I may have a naive question but eh..;depends on planes right ? -let's imagine, the PM raise the flaps instead of gear (on 787). Is it really a big issue that could lead to a lose of 200/300 feet ? I mean, you still have take of power ar at least climb power right ? sure you decrease the lift by raising the flaps (at constant speed though ) and lose some height, but the plane keep accelerating ,? 1 user liked this post. |
gearlever
2025-06-14T07:29:00 permalink Post: 11901200 |
hello guys,
I'm pilot but not on a heavy one, so I may have a naive question but eh..;depends on planes right ? -let's imagine, the PM raise the flaps instead of gear (on 787). Is it really a big issue that could lead to a lose of 200/300 feet ? I mean, you still have take of power ar at least climb power right ? sure you decrease the lift by raising the flaps (at constant speed though ) and lose some height, but the plane keep accelerating ,? |
FullWings
2025-06-14T07:36:00 permalink Post: 11901205 |
Only on the electrically-powered centre system (which does gear and flaps). Left and right have engine-driven pumps which will provide plenty of power for flight controls provided the engines remain above maybe 30-40% N2.
Compromising both engines inherently compromises the electrical system: dropping below idle N2 (plus some safety margin) disconnects generators. 3 users liked this post. |
FullWings
2025-06-14T08:09:00 permalink Post: 11901235 |
hello guys,
I'm pilot but not on a heavy one, so I may have a naive question but eh..;depends on planes right ? -let's imagine, the PM raise the flaps instead of gear (on 787). Is it really a big issue that could lead to a lose of 200/300 feet ? I mean, you still have take of power ar at least climb power right ? sure you decrease the lift by raising the flaps (at constant speed though ) and lose some height, but the plane keep accelerating ,? |
KSINGH
2025-06-14T08:43:00 permalink Post: 11901266 |
I’m not a 787 driver so for fear of looking dumb in front of those that are this still confuses me. Even IF they’ve mis-selected the flap setting (I still don’t think it’s been cemented on here that there is in fact a FMS/flap setting disagreement warning but i believe there is), had the wrong de-rated take off settings, selected flaps instead of gear up the 787 with massive high bypass engines, FBW and full envelope protections surely cannot let itself be put in such a low energy/high alpha regime as we saw in the videos IF it has both fans functioning normally, surely? the pilots may have messed up royally and numerous times so those holes lined up but the plane is the final block in the chain and a 21st century all digital entirely clean sheet design was sold as being immune to such catastrophic outcomes from a few minor (consequential yes) and fairly common errors- aren’t all the protections and our procedures designed after decades of mistakes? im having a hard time squaring how a fully functioning modern bird like this could allow for this outcome and almost whatever the pilots did outside of unbelievable inputs and the pilots are are a bit of a red herring IMO ![]() Dale Winsley @Winsleydale No. The LE slats are deployed therefore the flaps are as well. This is an automatic linkage. The flaps are set at Take-Off. Hard to see from the angle but they are...if slats are out (easy to see) then flaps are set. Looks like Flaps 5. Also, the 787 has the highest Thrust-to-Weight ratio of any airliner on Earth. The change in Alpha and lift is a trifling matter for it, at these settings (1-5). It will fly out of it easily, even at that density altitude. The attitude change is - in the circumstances I describe, consistent with a massive power loss (both sides). I believe based on probability that simultaneous mechanical failure is not the cause. Fuel contamination or starvation is likewise unlikely based on the 787 fuel system. The common element is the FADEC/Autothrottle/TOGO. However, each engine FADEC is dual redundant two channels. So any such common failure must happen further upstream. From a design perspective, that would be unthinkable. But this is Boeing. Given what I can see with my own eyes, I believe the flap issue is a non-starter. Also, re the landing gear: Clearly the Positive Rate challenge would be met based on normal rotation and fly-off at V2. But since we know the flaps were set correctly, that rules out an "oopsie" moment. Just as likely there was at the challenge moment an indication that something was amiss, and the Gear Up call was not made. They see both N1s unwinding and it takes a second to get past the WFT factor. They cross-check and see the airspeed also unwinding. Then they unload the Alpha and pitch to gear down Vy. And they had another 6 seconds. Whatever it was, it was not a flap, mechanical or fuel issue. We will know soon enough. But this is Boeing. My gut says "software". All 787s worldwide need to be grounded, now. 6:10 AM \xb7 Jun 14, 2025 \xb7 53.8K Views Last edited by Senior Pilot; 14th Jun 2025 at 09:04 . Reason: Add X quote |
KSINGH
2025-06-14T08:52:00 permalink Post: 11901272 |
https://x.com/winsleydale/status/193...230524974?s=46
I\x92m not a 787 driver so for fear of looking dumb in front of those that are this still confuses me. Even IF they\x92ve mis-selected the flap setting (I still don\x92t think it\x92s been cemented on here that there is in fact a FMS/flap setting disagreement warning but i believe there is), had the wrong de-rated take off settings, selected flaps instead of gear up the 787 with massive high bypass engines, FBW and full envelope protections surely cannot let itself be put in such a low energy/high alpha regime as we saw in the videos IF it has both fans functioning normally, surely? the pilots may have messed up royally and numerous times so those holes lined up but the plane is the final block in the chain and a 21st century all digital entirely clean sheet design was sold as being immune to such catastrophic outcomes from a few minor (consequential yes) and fairly common errors- aren\x92t all the protections and our procedures designed after decades of mistakes? im having a hard time squaring how a fully functioning modern bird like this could allow for this outcome and almost whatever the pilots did outside of unbelievable inputs and the pilots are are a bit of a red herring IMO 2 users liked this post. |
directsosij
2025-06-14T11:55:00 permalink Post: 11901403 |
https://x.com/winsleydale/status/193...230524974?s=46
I\x92m not a 787 driver so for fear of looking dumb in front of those that are this still confuses me. Even IF they\x92ve mis-selected the flap setting (I still don\x92t think it\x92s been cemented on here that there is in fact a FMS/flap setting disagreement warning but i believe there is), had the wrong de-rated take off settings, selected flaps instead of gear up the 787 with massive high bypass engines, FBW and full envelope protections surely cannot let itself be put in such a low energy/high alpha regime as we saw in the videos IF it has both fans functioning normally, surely? the pilots may have messed up royally and numerous times so those holes lined up but the plane is the final block in the chain and a 21st century all digital entirely clean sheet design was sold as being immune to such catastrophic outcomes from a few minor (consequential yes) and fairly common errors- aren\x92t all the protections and our procedures designed after decades of mistakes? im having a hard time squaring how a fully functioning modern bird like this could allow for this outcome and almost whatever the pilots did outside of unbelievable inputs and the pilots are are a bit of a red herring IMO of course like everyone else I have absolutely no idea what actually happened but I am willing to bet the explanation will be simpler than everyone is expecting. I am not going to speculate further as I believe it is a waste of time without further information. For the record I am not b787 rated but I do have Boeing and airbus narrow body and wide body time and i struggle to forsee a situation where the aircraft falls out of the sky at 200ft without a very serious error of some description. 3 users liked this post. |
MR8
2025-06-14T12:31:00 permalink Post: 11901444 |
Even though there is no point speculating about the cause of this accident, it is the nature of the beast to have questions. As pilots (most of us at least), we do have an inquiring mindset.
My initial thoughts were an inadvertent flap retraction. But with the ‘evidence’ that has been presented over the last 48 hours, I think we can safely discard that option. What we think we know is: - RAT was deployed (highly possible) - Gear was selected up, but did not operate (bogey tilted, doors remained closed) - APU was ‘on’ (APU door open on after crash pictures) - Flight path Any of these observations, alone, would mean very little. However, in combination, they all point to a dual engine flameout just at/after the rotation. The aircaft has enough kinetic energy to reach roughly 150ft altitude, and then starts a shallow descent at ‘alpha max’ into the buildings ahead. The RAT deployed, APU attempted auto-start, gear was unable to retract. I only wonder why the engines spooled down. Bird strike seems to be out of the question, so that leaves us with only a very few options, which include a software bug or a suicidal pilot (not a popular option, I understand, but we have to take all options into account). What I don’t believe is incorrect FCU selections, since that would not explain the high AOA on impact. It also would not explain the RAT, no gear retraction or the APU inlet flap open. Another thing that is highly unlikely is any switching done by the pilots, especially RAT etc.. The airborne time is just too little, pilots usually don’t take any action below approximately 400ft, and these switches are so ‘underused’ that a pilot would not find them instantaneously in a high stress situation. For me, a dual engine flameout seems the only possible explanation, now we only have to wait for its cause. 16 users liked this post. |
OPENDOOR
2025-06-14T12:43:00 permalink Post: 11901451 |
Even though there is no point speculating about the cause of this accident, it is the nature of the beast to have questions. As pilots (most of us at least), we do have an inquiring mindset.
My initial thoughts were an inadvertent flap retraction. But with the ‘evidence’ that has been presented over the last 48 hours, I think we can safely discard that option. What we think we know is: - RAT was deployed (highly possible) - Gear was selected up, but did not operate (bogey tilted, doors remained closed) - APU was ‘on’ (APU door open on after crash pictures) - Flight path Any of these observations, alone, would mean very little. However, in combination, they all point to a dual engine flameout just at/after the rotation. The aircaft has enough kinetic energy to reach roughly 150ft altitude, end then starts a shallow descent at ‘alpha max’ into the buildings ahead. The RAT deployed, APU attempted auto-start, gear was unable to retract. I only wonder why the engines spooled down. Bird strike seems to be out of the question, so that leaves us with only a very few options, which include a software bug or a suicidal pilot (not a popular option, I understand, but we have to take all options into account). What I don’t believe is incorrect FCU selections, since that would not explain the high AOA on impact. It also would not explain the RAT, no gear retraction or the APU inlet flap open. Another thing that is highly unlikely is any switching done by the pilots, especially RAT etc.. These airborne time is just too little, pilots usually don’t take any action below approximately 400ft, and these switches are so ‘underused’ that a pilot would not find them instantaneously in a high stress situation. For me, a dual engine flameout seems the only possible explanation, now we only have to wait for its cause. ![]() Last edited by Senior Pilot; 14th Jun 2025 at 19:08 . Reason: Double posting of image |
aeo
2025-06-14T14:05:00 permalink Post: 11901513 |
I agree it is helpful to seek a consensus on some of these matters.
The most productive responses would be along the lines of:- (1) I too have read all previous posts and agree that your summary reflects the current consensus, (2) I too have read all previous posts and agree your summary reflects the consensus HOWEVER I challenge that consensus because... [ [i]EITHER (a) reference to previous post that merits greater credence, OR (b) new evidence supplied], (3) I too have read all previous posts but I do NOT agree your summary reflects the consensus [explanation required]. It is not necessary for everyone who thinks (1) to say it (although some initial feedback would be useful!). However, if any of the more experienced and informed PPRuNers are thinking either (2) or (3) then it would be instructive to hear that. FWIW, yours strikes me as a reasonable summary of the best consensus I have been able to discern (as of ~30 minutes ago). There are multiple caveats to each line item, but I presume you've deliberately left those out for the sake of readability, so I'll do the same! The only comments I would add are:- - It's a stretch to say the RAT is seen or heard "conclusively". Doubts have been expressed about the video quality and there are dissenting views regarding the audio. If a few more people were able to wade in on the audio point in particular, this could be very beneficial in moving the discussion forward because the presence or otherwise of the RAT is significant to several competing theories. - On the subject of audio, I am surprised there has not been more discussion regarding engine noise. In the primary eye witness video the (alleged) RAT can be heard distinctly, as can the sounds of distant impact. If the engines were working as expected when overflying the camera and then flying directly away from it, do we really not think the engine noise would be more conclusive, i.e. louder (notwithstanding quiet engines and derated takeoffs)? Whichever way readers are leaning in the flaps versus power loss debate, surely these two points are pivotal, and we have actual evidence available to discuss? - Gear bogies: I'm not sure a consensus has yet been reached regarding the angle of the bogies. (I am not personally qualified to comment on this - I am purely saying I don't see a clear consensus just yet among those who are) - Mayday call: I don't recall seeing a confirmed source for the widely reported mayday. Others have brought this up in the thread but nobody appears to be able to confirm one way or the other. If accurate, its contents are informative. Am I right to presume that you have left it out of your summary due to a lack of confirmation? - The bogie could be explained by the Flap/Slat priority valve giving priority to the flaps if the PM suddenly realised his mistake and quickly put the flap lever back to the TO position and then selected the gear lever to UP. Those systems are both heavy hitters and would\x92ve sucked the life out of the CTR hydraulic system pumps. - There is no way loss of AC (alleged RAT deployment) could've caused a spool down of both engines. Think QF A380 incident in SIN - The entire #1 engine wiring harness in the wing was completely severed and yet it continued (by design) to run at its previous thrust setting. They had to shut it down using a fire truck! - History and design would dictate that a big 180 minutes ETOP\x92s twin such as the 787 having a dual engine failure or significant power loss at such a critical phase of flight would be a billion to one chance at best. Only the Airbus A400 had a software issue causing all 4 engine fuel shutoff valves to close causing it to crash killing the flight test crew - But this was during its development and flt testing. - Wide body twin\x92s delivering in the region of 60,000 to 115,000 lbs of thrust at TO rarely , if at all, flame out from multiple bird strike(s) like the baby Bus\x92s and Boeing\x92s. If anyone has seen the frozen chickens at TO power video would know what I\x92m talking about. And the Fan Blade being \x91blown off\x92 as well. In both cases the engine was was able to maintain full TOGA thrust for significantly longer than the AI aircraft. But it\x92s early days and anything could happen. And nothing surprises me anymore. 3 users liked this post. |
Alty7x7
2025-06-14T14:09:00 permalink Post: 11901517 |
Max EGzt and autorelight
Combining all the bits and pieces of info from this thread so far, IMO we can theoretically sequence it thus using the video from the left:
00:18 Rotation. Normal takeoff config. 00:24 Gear up starts. per Raffael with FF. ......... FR24 ADSB last transmission (71ft, 172kt) just before runway threshold. Matches with video aircraft altitude at 1/2 wingspan. ......... ? Full power flameout leaves N2 ~ 60%; Airspeed < 200k so N2 will decay to 15% in 8-10s? ......... ? Takeoff EGT of 900C needs 25-35s to fall below 250C ? 00:27 Gear up stops. per Raffael with FF. Bogies tilted. ......... ? APU starts. 20-55s to 95%N? ......... Per 787 dual-engine fail/stall memory items, PM initiates Fuel Cutoff and Run. 00:28 Visible loss of thrust. Alt ~ 200ft using aircraft wingspan as measure. ......... Matches with eyewitness "within 5-10s ... it was stuck in the air". ......... Per 787 dual-engine fail/stall memory items, PM initiates RAT Switch for 1s. Whether auto or manual, the RAT initiates. ......... RAT "bang" heard by survivor ......... RAT coming online accounts for eyewitness "lights started flickering green and white". ......... Per 787 QRH below 1000ft, PF makes no change to Main Landing Gear and flaps, aircraft pointed straight for best glide. 00:31 Descending visibly, somewhere beyond the runway threshold. Alt ~ 200ft using aircraft wingspan as measure. ......... ? Because EGT > 250C FADEC blocks fuel (T-HOT hot restart inhibit?) so no relight though N2 > 15% ? ......... 787 glide ratio between 16:1 to 25:1 with MLG down, Flaps 5. About 15-20s and 3-5000ft of glide from 200ft? ......... Some flap accounts for the ground pictures. 00:34 ? N2 has presumably decayed to 15%, FADEC flips to X-START: airspeed outside envelope? No hope of relight now. ......... PM/PF transmits Mayday? ......... Video showing RAT deployed. 00:46 APU reaches some fraction of 95%N (APU sound accounting for survivor's perception of thrust?). 00:48 Impact. 4200ft from descent start, 3990ft from airport boundary road. 17s from visible descent start. if this is a valid sequence, the only remaining question is why the dual-engine failure at ~200ft agl? with condolences to the families and people affected. In-flight, the Autorelight function should attempt to restart the engine as soon as a flameout is detected, and for an engine flaming out at high power it might catch it before it even goes sub-idle. Generally, Autorelight will continue attempting until some cutoff N2 at which time it will stop attempting, or if the pilot move the fuel switch to Cutoff. And while the EEC is still powered (via its own PMA) down to roughly 10% N2, the ignition exciters required for Autorelight do get their power from the airplane. |
njc
2025-06-14T15:06:00 permalink Post: 11901555 |
- The bogie could be explained by the Flap/Slat priority valve giving priority to the flaps if the PM suddenly realised his mistake and quickly put the flap lever back to the TO position and then selected the gear lever to UP. Those systems are both heavy hitters and would’ve sucked the life out of the CTR hydraulic system pumps.
- There is no way loss of AC (alleged RAT deployment) could've caused a spool down of both engines. Think QF A380 incident in SIN - The entire #1 engine wiring harness in the wing was completely severed and yet it continued (by design) to run at its previous thrust setting. They had to shut it down using a fire truck! - History and design would dictate that a big 180 minutes ETOP’s twin such as the 787 having a dual engine failure or significant power loss at such a critical phase of flight would be a billion to one chance at best. Only the Airbus A400 had a software issue causing all 4 engine fuel shutoff valves to close causing it to crash killing the flight test crew - But this was during its development and flt testing. - Wide body twin’s delivering in the region of 60,000 to 115,000 lbs of thrust at TO rarely , if at all, flame out from multiple bird strike(s) like the baby Bus’s and Boeing’s. If anyone has seen the frozen chickens at TO power video would know what I’m talking about. And the Fan Blade being ‘blown off’ as well. In both cases the engine was was able to maintain full TOGA thrust for significantly longer than the AI aircraft. As for history and design making a dual-engine failure a billion to one chance: I'd be more inclined to agree that it's unlikely to be what happened if the actual manufacturing of planes (Boeings in particular) and the maintenance procedures were both carried out "by the book" at all times by the manufacturer and the airlines... This is clearly not the case though. Last edited by Saab Dastard; 14th Jun 2025 at 19:35 . Reason: reference to deleted posts removed |
appruser
2025-06-14T17:21:00 permalink Post: 11901674 |
This is what he said - the PF *has* to push the nose down to prevent a stall and keep the aircraft flying, and if the PF won't, the aircraft will do so to prevent a stall. How much depends on the flap setting. |
Someone Somewhere
2025-06-14T17:35:00 permalink Post: 11901681 |
What concerns me a little bit is if indeed AC power is lost, would the suction feed inlets in the wing tanks provide enough fuel flow to maintain TO thrust?
I know the system is designed to achieve this in a situation where all of the AC powered boost pumps are lost. But what about in a real situation... Could this cause a degradation of thrust? Even the slightest decrease..
I did read and search this thread, but I found nothing about ADS-B loss just before the end of the runway and at 71 ft high, according to FR24. ADS-B coverage is poor on the ground on the north-east part of the airfield (hence the fake news about taking off from the intersection) but I don't think it would be lost once airborne, except if it has been shut off... electrical failure ?
more precisely, loss of the two Main AC buses (ADS-B not powered by Standby AC) There's a list of equipment operable on battery/RAT here, but I'm not sure which (if any) is the transponder (26:10): If you had gear pins and an engine loss, I could maybe see climb rate being zero or slightly negative. Not the brick impression we see here.
There have been a couple comments regarding the tilt of the bogies not corresponding to the landing configuration which have taken this as an indicator for an attempted (but failed) retraction.
I don't think anybody has so far confirmed which of the two positions the bogie would have without hydraulic pressure, but I would strongly think it is the one used in the retraction/extension cycle and not the landing configuration, for the simple reason that otherwise the gravity drop would potentially not work (I assume it is tilted for the stowing because it would otherwise not fit). Maybe someone with concrete knowledge can confirm this? This would then only confirm that the bogies were unpressurized (likely because of loss of hydraulics, but of course could also still be a partial retraction that stopped for some reason) 2 users liked this post. |
Fly-by-Wife
2025-06-14T19:12:00 permalink Post: 11901744 |
Studies show that for aircraft landing with engines at landing thrust, 30 - 50% of the noise generated is from the landing gear and flaps down, so if the aircraft here had engines at low thrust setting, as appears to be the case, then the sound heard approaching could have been in large part due to the landing gear and flaps, which were down. 3 users liked this post. |
Shep69
2025-06-14T19:26:00 permalink Post: 11901751 |
We're all shouting each other down with two main different theories on why the aircraft lost lift so shortly after takeoff.
1) Incorrect flap retraction causing the aircraft to lose lift and unable to recover the energy in time. (Not unheard of and plenty of reports where this has happened - albeit usually not to a crash). 2) Loss of engine thrust backed up two potential pieces of evidence that back up the RAT was deployed (apparent RAT sound, potential RAT seen on low res video). It is impossible to know which of these is the case. Considering this summary of memory items is there the potential for a combination of both theories to have taken place? Inadvertant flap retraction by PNF leading the PF to sense a sink and loss of lift. Pushes the thrust levers forward to the firewall and still the aircraft sinks. PF looking through the HUD and so very much 'outside focused' and doesn't realise that PNF has instead moved the flaps. PF defaults to memory items for loss of thrust on both engines before PNF can realise or communicate to PF what they've done, start switches are cut off which drops the RAT and from that point they're only heading one way. This would satisfy the strongly held belief that the RAT was extended, whilst also following the more likely initial cause of an action slip by PNF starting the sequence, rather than a dual engine failure. On a flap 5 takeoff the FMS could be programmed to select climb power at flaps 1 which would seem like an apparent loss of thrust. Same as for F15 to F5 or further. I`m not sure if they would have cycled the FCS switches or not. But the airplane certainly would have experienced a loss of lift would the flaps been inadvertently retracted. As well as perceived loss of thrust. OTOH any castastophic failure which left the gear down would have essentially left the flaps where they were. They are hydraulically activated with electrical backup but it`s wayyyyy slow. |
Tech Guy
2025-06-14T19:49:00 permalink Post: 11901771 |
So I called a 787 Captain to ask him about this - in dual-engine fail, at 200ft or below, 170kts, flaps 5, does the PF push the nose down for best glide, do nothing, or push nose up in transition to flare?
This is what he said - the PF *has* to push the nose down to prevent a stall and keep the aircraft flying, and if the PF won't, the aircraft will do so to prevent a stall. How much depends on the flap setting. It is also interesting to note that on Google maps, the crash location has been marked. If the aircraft flew another 300m, they would have crashed into the cities hospital. Could the pilot in his last moments have been trying to avoid that scenario? https://maps.app.goo.gl/zSyU8Y6A7AMS9FWy5 1 user liked this post. |
Shep69
2025-06-14T19:55:00 permalink Post: 11901777 |
Climb Power is programmed as an altitude in the FMC, usually 1000' but sometimes higher for noise abatement, which in this case they wouldn't have reached.
In some instances, the TO derate is so significant that the selection of climb power moves the thrust levers forward. AMD is sea level with a long runway, so can imagine it would be a fairly low power take off. And yes with a takeoff with heavy derates CLB might be more than selected for TO (although IIRC CLB2 usually wasn`t when we were using TO2 with moderate AT). Understand it`s a long runway but I wouldn’t assume heavy derates with a moderately long flight and full airplane (and hot day). But we don`t know yet. |
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