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appruser
July 16, 2025, 01:55:00 GMT permalink Post: 11923383 |
Since the preliminary report neglected including when the RAT deployment occurred, I've tried to estimate it based on the picture they did include:
![]() Baro altitude should be around 150ft; using the public cctv video, I estimate this picture was taken between 4-7 seconds after rotation. A wide range, but that was the best estimate I could come up with. Maybe someone else could narrow it down further. 1. ADSB readouts - according to FlightRadar24, the last ADSB transmission was at 71ft AGL. Is that significant given the RAT is seen already deployed at 150ft AGL per the estimate above? At 71ft AGL, the wheels are about 40-50ft off the ground, assuming aircraft attitude is unchanged between there and this image. Is that 1 or 2 seconds after rotation? Does this imply electrical issues? 1a. The timings for ADSB transmissions outlined by MrShed are not in sync with the estimates above - people have talked about a time shift in this thread. I do believe ADSB timestamps are by the receiving station. 2. The preliminary report timings from the EAFR for E2 fuel cutoff switch RUN -> CUTOFF to the RAT supplying hydraulic power disagree with the lower end of the 4-7s estimate above, and are only consistent if this picture was taken 6-7 seconds after rotation, in my opinion, because of the time (4-5s) it would take to cut off the fuel to E2, spool down to where the VFSGs stop providing AC power, and RAT deployment. 3. The Preliminary Report mentions that the RAT deployed "immediately after" lift-off. Again, I have to wonder, why didn't they provide the RAT deployment timestamp, even relative to rotation? If this is in fact the case, does this imply electrical issues, in line with the last ADSB altitude reading? FR24 article https://www.flightradar24.com/blog/f...rom-ahmedabad/ Last edited by appruser; 16th July 2025 at 01:57 . Reason: Added link to FR24 blog post |
Musician
July 16, 2025, 03:52:00 GMT permalink Post: 11923409 |
This was posted sometime ago, but if anyone would still find it useful to pinpoint the location of the aircraft in the 'new' photo from the Preliminary Report (with RAT deployed) I made a crude attempt which placed it roughly midway between the two sets of identical touchdown zone markings, ~245m (803 ft) from the displaced threshold of RW05.
The deemed position of the CCTV camera is only an estimate, based on visual cues. I'm happy to share my workings, should anyone find it useful to cross-reference this with other data they are working on, but I will avoid cluttering up the thread any further until/unless it becomes relevant. You're looking for the point where the LEFT of the two white lines intersects the runway (ignore the white dots): ![]()
Generally don't think it's a good idea to reply to own posts, but in this case wanted to keep things in context. A few interesting items of note:
1. ADSB readouts - according to FlightRadar24, the last ADSB transmission was at 71ft AGL. Is that significant given the RAT is seen already deployed at 150ft AGL per the estimate above? At 71ft AGL, the wheels are about 40-50ft off the ground, assuming aircraft attitude is unchanged between there and this image. Is that 1 or 2 seconds after rotation? Does this imply electrical issues? 1a. The timings for ADSB transmissions outlined by MrShed are not in sync with the estimates above - people have talked about a time shift in this thread. I do believe ADSB timestamps are by the receiving station. 2. The preliminary report timings from the EAFR for E2 fuel cutoff switch RUN -> CUTOFF to the RAT supplying hydraulic power disagree with the lower end of the 4-7s estimate above, and are only consistent if this picture was taken 6-7 seconds after rotation, in my opinion, because of the time (4-5s) it would take to cut off the fuel to E2, spool down to where the VFSGs stop providing AC power, and RAT deployment. 3. The Preliminary Report mentions that the RAT deployed "immediately after" lift-off. Again, I have to wonder, why didn't they provide the RAT deployment timestamp, even relative to rotation? If this is in fact the case, does this imply electrical issues, in line with the last ADSB altitude reading? FR24 article https://www.flightradar24.com/blog/f...rom-ahmedabad/ Note that the good folks at FR24 did not apply temperature correction to the barometric altitude (they corrected for air pressure and runway elevation); pilots on pprune have done the corrections themselves and arrived at slightly different values, so take those altitude numbers with a grain of salt. Note also that the 787 sends altitude in 25 ft. increments, and I don't know how these are rounded (up, down, nearest). We do not know how long the RAT has been deployed in this photo, we only know it can't have been deployed later. I have learned on this thread that the CUTOFF switch will also cause the VFSGs to disconnect, i.e. the B787 systems will electrically isolate the engine from the power buses before it has spooled down. With a dual failure, this would leave the main buses unpowered in short order, so if all of this is correct, the RAT would have clonked into place very soon after the second engine was cut off. This would not depend on the turbine speed. I personally do not know what items are logged on the flight recorder, but I imagine RAT deployment was not among them. If so, the conditions for its deployment would be logged, but it requires an analytical step to conclude it did, and a preliminary report typically has no analysis at all. Hydraulic pressure to the flight controls is likely logged, so the RAT delivering hydraulic power would be a matter of record. Where is the RadAlt antenna on a 787? Is it in the nose, or further back between the main gears? Last edited by Musician; 16th July 2025 at 04:02 . |
Chiefttp
July 17, 2025, 21:23:00 GMT permalink Post: 11924674 |
DMBA,
You posted, “what about a flying jam donut depositing monkey toes on the control switches and causing them to lift up by using elephants to fly up and over the lock? Can you rule that out? No, so maybe it happened… let’s get real! Such a strange response, I’m not disputing that someone physically shut off the Fuel Control Switch. I’m sayin possibly he did it by mistake in a confused state. I’ve seen it myself, where a 60 year old pilot tried to shut off a hydraulic pump on the left side of the cockpit (he was an F/O sitting right seat) when the checklist called for shutting off a Pack directly above his head. They are not even close, and he was diagnosed with early onset Alzheimer’s. His erratic and confused action caused him to fail the ride. Why is my theory so off the wall, but the fact that he wanted to commit suicide, and take hundreds of innocent people with him considered plausible? Are you a pilot? |
Sailvi767
July 18, 2025, 01:32:00 GMT permalink Post: 11924794 |
Apologies for the delay in responding to your posts. I see that you and others have stepped in, thanks.
I think for various reasons the ADSB data's absolute values are offset by some amount, for possibly all of the parameters. But there should be consistency in the deltas for the timestamp (by receiving station), the raw baro altitude, the Flightradar24 AGL values, and the airspeed. Flightradar24 themselves note that for altitude " ... the data is not above ground level, but it is consistent to itself." 08:08:46.55 ... 575ft ... 21ft ... 184kt 08:08:48.14 ... 600ft ... 46ft ... 179kt 08:08:48.61 ... 600ft ... 46ft ... 177kt 08:08:49.01 ... 600ft ... 46ft ... 177kt 08:08:49.46 ... 625ft ... 71ft ... 177kt 08:08:49.92 ... 625ft ... 71ft ... 174kt 08:08:50.39 ... 625ft ... 71ft ... 174kt 08:08:50.87 ... 625ft ... 71ft ... 172kt From the Preliminary Report's airport cctv picture, the RAT was seen deployed at, by my estimate here , 150ft baro altitude, between 4-7 seconds after rotation. So the ADSB readings have to be prior to that. What's interesting is that the ADSB data covers: - 4-5 seconds of time (let's approximate 4 seconds from 46.55 to 50.55, ignoring the 0.32s for the moment) - 50ft of altitude gain - Declining airspeed from the 1st reading to the last in this final segment from the runway. Big questions in my mind: 1. If the loss of ADSB corresponds to the E1/E2Fuel Cutoff switches being moved from RUN -> CUTOFF, why is the airspeed declining for the prior 4 seconds? 2. In 4 seconds, why is there only 50ft of altitude gain? that seems odd. 3. To account for only 50ft of alt gain, if we assume the 1st reading is on the runway just before rotation, the intermediate +25ft alt gain is at rotation (Nose up but MLG still on the runway), and the last 4 readings are in the air (nose up an additional 25ft), that means that 1 second or less after lift-off, ADSB was lost - this is before E1/E2 FCO RUN-> CUTOFF. It's just weird . The widely watched video shows a very normal initial rotation and climb. |
appruser
July 18, 2025, 03:43:00 GMT permalink Post: 11924815 |
I am not sure why 50 feet in 4 seconds seems odd right after liftoff in a heavy aircraft. That corresponds to 750 FPM. Seems entirely normal to me. The rate would have been increasing as the timeline advanced. I would also point out that RAT deployment verses the rat coming online fully are two different times. When that RAT is singled to deploy it bangs out nearly instantly. It begins producing its rated electrical and hydraulic power sometime after deployment.
The widely watched video shows a very normal initial rotation and climb. Since the preliminary report states E2 cutoff after 3-4 seconds after lift-off, if that cutoff corresponds to ADSB interruption and which itself was only transmitting for 4 seconds, then 50ft after liftoff is a bit anemic? But if we include the first 25ft after rotation but before lift-off, then, because the ADSB duration is only 4 seconds, it means that ADSB was interrupted before the E2 FCO operation. I don't know if there is a sliding window - part after rotation, part after lift-off that might meet all of these constraints. That still leaves unexplained the declining airspeed seen in the ADSB data... did prior discussions on the ADSB data cover this? is there a good explanation? Last edited by appruser; 18th July 2025 at 04:03 . Reason: fixed heights |