Page Links: First Previous 1 2 Last Index Page
M2dude
December 04, 2010, 08:17:00 GMT permalink Post: 6101395 |
Bellerophon
Deciding that they would like to maintain this groundspeed, they went ALT HOLD and MACH HOLD at around FL530. They maintained their groundspeed, so the story goes, but the autothrottle then progressively reduced the N1, as the aircraft weight reduced, over the next couple of hours, into the prohibited range!Did you ever hear of any such event?
![]() ChristiaanJ
Can somebody explain to a "Volts and Amps and Ohms ancient" what "hotstreak injection" is/was (without getting scabrous)?
![]() The lighting of a reheat flame can be achieved in three ways: 1) By using an electric arc ignitor.. the least reliable system, although relatively simple in concept. 2) Catalytic ignition, where the reheat fuel is sprayed over a platinum based catalyst, spontaneously igniting. I recall that although generally reliable, eventually the catalyst compound erodes away and you are left with no ignition source. 3) Hot streak injection (or ignition). I this case a sizable jet of fuel is injected through a single injector placed the the combustion chamber of the engine, a powerful streak of flame then 'shoots out' of the turbine, and ignites the reheat fuel. Generally reliable as long as the injector itself does not carbon up (as our new friend Howiehowie93 pointed out). What amazed me with this system when we were looking at it for Concorde, was that the Olympus 593 designer I spoke to at Rolls-Royce told me that it has a negligible effect on turbine blade life, as the hottest part of the flame does not hit the blades themselves, and also of course it is a very short duration burn anyway (1 - 2 seconds). And Christian my friend, you should indeed 'rabbit on' here about some of your observations regarding Concorde electronics technology, you have a unique insight here as (probably) the only Concorde systems designer that regularly visits 'here'. I'm sure I speak for many of us here when I say that your experiences are unique and your contributaions are always illuminating. Come on, let's have some Volts/Amps and Ohms ![]() Best Regards Dude ![]() Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
Landroger
December 05, 2010, 09:31:00 GMT permalink Post: 6103472 |
This thread just gets better.
A couple of observations and a questionette, if I may? First, I'm feeling quite pleased with myself that I have largely understood the latest phases of discussion, re: Reheat Ignition and N1 resonance! To be fair I was a bit puzzled about 'Hot Streak' until Dude explained in a slightly different way. Then my first thought was; 'Cor crikey, isn't there enough heat on the turbine blades already?' It seems not, but it does raise the issue of TBE (TEB?) injection,
a la
SR71? I know the Blackbird used rather different fuel (JP8?), but is there not a similar chemical that would have done the same thing? Perhaps it was a reluctance to use 'exotic' chemicals in a civilian aeroplane?
The resonance issue is quite interesting, in that it appears to have affected all models of Olympus and was at roughly the same rpm on all. I take it that any attempt to damp specific frequency resonance would have adversely affected the performance? Which brings me to my questionette - given that Bristol-Siddley created the original design when jet travel was still quite novel, what was it about the Olympus that made it so capable in so many guises and for so long? Not only Concorde of course, but TSR2, warships and fixed electrical generators. Roger. Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
Mr.Vortex
December 07, 2010, 21:18:00 GMT permalink Post: 6108984 |
Wow thanks a lot M2Dude for your diagram.
![]() I'm wonder that did Concorde has a neutal of stable stability? Did the elevon work out the same job to produce the stability like the elevator and stabilizer? Also, I have read your post and wonder why when the temp fall below ISA-7, the AICU order the N1 to decrese? And the final question. In the early concorde, does the pilot has ability to select the amount of afterburn thrust by rotate the area knob is that right? and why the airline remove it? Thanks for your reply. Best Regards Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
M2dude
December 08, 2010, 17:05:00 GMT permalink Post: 6110672 |
Landroger
Which brings me to my questionette - given that Bristol-Siddley created the original design when jet travel was still quite novel, what was it about the Olympus that made it so capable in so many guises and for so long? Not only Concorde of course, but TSR2, warships and fixed electrical generators.
howiehowie93
The Olympus - nowt ! Two Spools and a Fuel Valve thats your lot. nothing to go wrong and being an Aeroderivative all the ancillary equipment is either bolted on underneath or away from the engine outside the enclosure.
Was it all still BSF on the 593?
oh ! I forgot about the Hot Shot; when I was ground running installed RB199's there was no jump in TBT/T7, you couldn't sense it fire either, the only feel was either the Reheat lighting off with a big roar or the engine going quiet as the Nozzle opened up until the MECU noticed it hadn't lit and closed it again sharpish.
Tom355UK
How much would it cost, do you think, that IF EADS really wanted to, using a combination of all the knowhow gained through L'Oiseau Blanc and their current lineup could they produce a 'Concorde NG'? Most importantly, would there be a market for such a beast (at the right price)?
![]() Jeepers Tom that is one hell of a question. Assuming there was a market for such a venture (personally not sure right now) I think you are looking at BILLIONS of $, and for this reason alone I think you'd find that a multi-national/continental effort would be required. There is little doubt that technology is not the major barrier here, but economics and political will. (Nice thought though, I do agree). As far as a powerplant goes, well the PW5000 is a really superb engine, although well down on the thrust requirement for an 'NG' SST. More likely I would have thought would be e development of the Olympus, there was/is still such an enormous amount of potential in this basic design. (But who knows, this is all pure speculation anyway). And have no fears about posting here Tom, most of us are quite happy to answer away (We've said before that there is no such thing as a stupid question; you are most welcome here ![]() DavvaP
Ok, so my question is - BA had to use an airframe as a test for the modifications. However, the choice of airframe seemed a strange one to me, BOAF - which I previously thought to be one of the youngest and best airframe they had (m2dude you explained that BOAF and BOAG weighed less than the previous models). So, why would BA use one of their best airframes, rather than use perhaps the most worn out of their fleet?
I am honoured to say that I was lucky enough to be onboard G-BOAF for that flight from LHR-BZZ and as far as I could tell, the liners had no impact whatsoever. One amusing ![]() Those 7 aircraft really did look magnificent I know, it was just sad as to the reason they were all lined up there. Mr.Vortex
I'm wonder that did Concorde has a neutal of stable stability? Did the elevon work out the same job to produce the stability like the elevator and stabilizer?
Also, I have read your post and wonder why when the temp fall below ISA-7, the AICU order the N1 to decrese?
And the final question. In the early concorde, does the pilot has ability to select the amount of afterburn thrust by rotate the area knob is that right? and why the airline remove it?
![]() Best regards to all Dude ![]() Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
EXWOK
December 29, 2010, 10:21:00 GMT permalink Post: 6148025 |
That's a very 'Concorde' picture, Bellerophon.
Gentle descent in the crz, N1 max, N2 max, similar fuel burn per engine as a 747 (but over double the speed), Airspeed and Mach numbers just shy of the barber's poles, must have been well above FL500 given the Mach number yet the cabin alt is a smidge over 5000'. Elapsed time 1hr 31, Longitude over 41W. Took me over three hours to get to 40W yesterday....... PS and it has to be OAD, because for some reason the nose/visor control panel is black. I've no idea why I can remember stuff like that, but not the name of someone I met last week...... Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
M2dude
January 13, 2011, 08:45:00 GMT permalink Post: 6176684 |
atakacs
Just wondering was that the maximum speed "in" the design ? I understand that "the higher & the colder = the faster" was the key to the performance and that the Mach +/- 2.0 cruise was implied by limiting altitude to FL 600 in order to mitigate cabin depressurization consequences. I guess there where also thermal issues but was, say, Mach 2.2 @ FL700 "warmer" than Mach 2.0 @ FL600 ?
Really an answer for CliveL, but I'll have a go. The short answer to your question is 'oh yeah, big time'. Total temperature varies with the SQUARE of Mach number and static temperature. Depending on the height of the tropopause itself as well as other local factors, there can be little or no significant variation of static temperature between FL600 and FL700. The 400\xb0K (127\xb0C) Tmo limit was imposed for reasons of thermal fatigue life, and equates to Mach 2.0 at ISA +5. (Most of the time the lower than ISA +5 static air temperatures kept us well away from Tmo). In a nutshell, flying higher in the stratosphere gains you very little as far as temperature goes. (Even taking into account the very small positive lapse above FL 650 in a standard atmosphere). As far as the MAX SPEED bit goes, Concorde was as we know flown to a maximum of Mach 2.23 on A/C 101, but with the production intake and 'final' AICU N1 limiter law, the maximum achievable Mach number in level flight is about Mach 2.13. (Also theoretically, somewhere between Mach 2.2 and 2.3, the front few intake shocks would be 'pushed' back beyond the lower lip, the resulting flow distortion causing multiple severe and surges). On C of A renewal test flights (what I always called the 'fun flights') we DID used to do a 'flat' acceleration to Mach 2.1 quite regularly, as part of the test regime, and the aircraft used to take things in her stride beautifully. (And the intakes themselves were totally un-phased by the zero G pushover that we did at FL630). This to me was an absolute TESTAMENT to the designers achievement with this totally astounding aeroplane , and always made me feel quite in awe of chaps such as CliveL. ![]()
Also wondering what was the max altitude ? Was high altitude stall (for the lack of a better word) ever experimented during tests or training ?
Shaggy Sheep Driver So glad you are enjoying the thread, and absolutely loved the description of your flight in OAD and your photo is superb. I don't think it is possible to name a single other arcraft in the world that could be happily flown hands off like this, in a turn with 20\xb0 of bank at Mach 2. (One for you ChristiaanJ; The more observant will notice that we are in MAX CLIMB/MAX CRUISE with the autothrottle cutting in in MACH HOLD. Oh, we are in HDG HOLD too ![]() Now for your question
I understand that the anti-skid used a rotational reference from the unbraked nosewheels to compare to the rotation of the mains, and that with gear down in the air a substiute nose-wheel referance is supplied which, because the mains are not yet rotating, allows the anti-skid to keep the brakes off. But what happens when the mains touch down with the nose wheels still high in the air? What (if anything) inhibits wheel braking until the nosewhels are on the ground (and therefore rotating)?
As far as your air conditioning question goes, you needed an external air conditioning truck to supply cabin air on the ground. Not needed in the hangars of course, but come departure time if these trucks were not working, then the cabin could become very warm/hot place indeed (depending on the time of year). Oh for an APU ![]() Best regards Dude ![]() Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
CliveL
January 13, 2011, 10:10:00 GMT permalink Post: 6176851 |
Originally Posted by
M2Dude
Really an answer for CliveL, but I'll have a go. The short answer to your question is 'oh yeah, big time'. Total temperature varies with the SQUARE of Mach number and static temperature. Depending on the height of the tropopause itself as well as other local factors, there can be little or no significant variation of static temperature between FL600 and FL700. The 400\xb0K (127\xb0C) Tmo limit was imposed for reasons of thermal fatigue life, and equates to Mach 2.0 at ISA +5. (Most of the time the lower than ISA +5 static air temperatures kept us well away from Tmo). In a nutshell, flying higher in the stratosphere gains you very little as far as temperature goes. (Even taking into account the very small positive lapse above FL 650 in a standard atmosphere). As far as the MAX SPEED bit goes, Concorde was as we know flown to a maximum of Mach 2.23 on A/C 101, but with the production intake and 'final' AICU N1 limiter law, the maximum achievable Mach number in level flight is about Mach 2.13. (Also theoretically, somewhere between Mach 2.2 and 2.3, the front few intake shocks would be 'pushed' back beyond the lower lip, the resulting flow distortion causing multiple severe and surges).
On C of A renewal test flights (what I always called the 'fun flights') we DID used to do a 'flat' acceleration to Mach 2.1 quite regularly, as part of the test regime, and the aircraft used to take things in her stride beautifully. (And the intakes themselves were totally un-phased by the zero G pushover that we did at FL630) As usual Dude you beat me to it! I really must give up having another life ![]() As Dude says, the 'cruise' condition was set by the aircraft specification for transatlantic range on an 85% (ISA +5) day and the chosen mach Number was 2.0 (of which more anon). This gives a Total Temperature of 400.1 deg K. [Dude, I know your pipe-smoking thermodynamicist and he was having you on - he is quite capable of memorising the square/square root of 407.6 or whatever!] To give margins for sudden changes in ambient temperature (we had to cater for a 21 deg change in one mile) the Mmo was set at 2.04 which matches 400 degK at ISA +1. In theory then we could have flown faster than our chose Mmo at anything colder than this, but there are two limits: 1) The object is not to fly as fast as you can but to fly with minimum miles/gallon. If you have a nice cold day and enough thrust to go either faster or higher which do you choose? For best specific range you go higher every time. 2) The thing that everyone forgets is that civil aircraft have to have margins around their authorised envelope. In Concorde's case these were set principally by the intake limits and engine surge. Dude also says quite correctly that 101 flew to 2.23M but the production aircraft was limited to 2.13M. Now you may not believe this, but 101 could fly faster than the production aircraft because she (101) leaked like a sieve!. I doubt I will get away with that without some explanation ![]() Once you get past a certain Mach Number the airflow into the intake is fixed. The performance (intake pressure recovery and engine face flow distortion) then depends on how this air is shared between the engine and the throat 'bleed'. This bleed was ducted over the engine as cooling air and then exhausted (in principle) throught the annulus formed between the expanding primary jet and the fixed walls of the con-di nozzle. But if you took, or tried to take, more bleed air the intake pressure recovery went up and the primary jet pipe pressure went up with it. This meant that the primary jet expanded more and squeezed the available annulus area which restricted the amount of bleed air one could take. Obviously if there are alternative exit paths between intake and final nozzle then you can take more bleed air off and the engine face flow distortions will benefit along with the surge margin. 101 was fairly 'leaky' in this respect, particularly around the thrust reverser buckets on the original nozzle design. This meant that 101's intake distortions were lower than the production aircraft so she could fly faster without surge - at least with the first attempt at intake control 'laws'. We managed to tweak most of the margin back eventually. Engine bay leaks were good for surge margin but VERY bad news for m.p.g.! Here are a couple of diagrams to show what I mean. the first shows the surge lines for the various aircraft variants and also the N1 limiter Dude was talking about. NB: the X-axis is LOCAL Mach Number not freestream. The difference comes from the compression of the underwing flow by the bit of the wing ahead of the intake. Mmo + 0.2 is shown ![]() ![]() As for 'high speed stall', I don't think we ever contemplated trying it! Our requirements in 'g' capability were defined and that was it. Besides, the aircraft would fly like the proverbial stone-built outbuilding at those sorts of conditions so I don't think one would have been able to get anywhere near a stall in the conventional sense. Stall as commonly defined for subsonics (deterrent buffet) might have been another matter, but I don't remember anything. Cheers Last edited by CliveL; 13th January 2011 at 10:17 . Reason: additional explanation Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
Quax .95
April 06, 2011, 18:43:00 GMT permalink Post: 6354590 |
Hello skyhawkmatthew!
M2dude gave a good answer on your question in post #1085, so I think I may quote this here again.
Originally Posted by
M2dude
As far as the MAX SPEED bit goes, Concorde was as we know flown to a maximum of Mach 2.23 on A/C 101, but with the production intake and 'final' AICU N1 limiter law, the maximum achievable Mach number in level flight is about Mach 2.13. (Also theoretically, somewhere between Mach 2.2 and 2.3, the front few intake shocks would be 'pushed' back beyond the lower lip, the resulting flow distortion causing multiple severe and surges).
The maximum altitude EVER achieved in testing was I believe by aircraft 102 which achieved 68,000'. Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
Quax .95
April 07, 2011, 19:56:00 GMT permalink Post: 6356891 |
Not quite right: the reheats ignite if
(At temperatures colder than -35\xb0C the engine control schedule limits the N1 of all engines to 88% or less.)
Originally Posted by
Brit312
Up to 60 kts the F/E could reselect a failed reheat so hoping it would be OK by 100kts
Last edited by Quax .95; 11th April 2011 at 15:34 . Reason: T/O-case added Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
Quax .95
April 07, 2011, 21:15:00 GMT permalink Post: 6357012 |
This might be because the #4 engine accelerates less fast than the others due to the limiter, reaching 81% N1 a little bit later. But this thread is too brilliant for presumptions (don't want to repeat the mistake of my first post...
![]() Last edited by Quax .95; 8th April 2011 at 22:53 . Reason: spelling Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
M2dude
April 08, 2011, 06:13:00 GMT permalink Post: 6357473 |
Jane-DoH
One of the real beauties of the Concorde intake was that it was completely self-startiing, and so unstarts as such were never heard of. Regarding the vibrations thing, here is my post #80:
The reason that #4 engine was limited to 88% N1 on take-off was an interesting one, down to something known as 'foldover effect'. This was discovered during pre-entry into service trials in 1975, when quite moderate levels of first stage LP compressor vibrations were experienced at take-off, but on #4 engine only. Investigations revealed that the vibrations were as the result of vorticies swirling into #4 intake, in an anti-clockwise direction, coming off the R/H wing leading edge. As the engine rotated clockwise (viewed from the front) these vorticies struck the blades edgewise, in the opposite DOR, thus setting up these vibrations. The vorticies were as a result of this 'foldover effect', where the drooping leading edge of the wing slightly shielded the streamtube flowing into the engine intake. #1 engine experienced identical vorticies, but this time, due to coming off of the L/H wing were in a clockwise direction, the same as the engine, so were of little consequence. It was found that by about 60 KTS the vorticies had diminished to the extent that the N1 limit could be automatically removed. Just reducing N1 on it's own was not really enough however; some of this distorted airflow also entered the air intake through the aux' inlet door (A free floating inward opening door that was set into the spill door at the floor of the intake. It was only aerodynamically operated). The only way of reducing this part of the problem was to mechanically limit the opening angle of the aux' inlet door, which left the intake slightly choked at take off power. (The aux' inlet door was purely aerodynamically operated, and diff' pressure completely it by Mach 0.93).
Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
M2dude
April 08, 2011, 15:29:00 GMT permalink Post: 6358344 |
For take-off reheat was selected (armed) on all 4 engines together, and certainly not in pairs. (As was stated previously, once 81% N1 was reached the reheat light-up sequence was automatically initiated). You would not wind up on the brakes either, the carbon brakes were extremely sensitive to overtorquing. For transonic acceleration however you are quite right about the 'burners in pairs' bit.
Last edited by Jetdriver; 10th April 2011 at 08:23 . Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
asc12
September 09, 2011, 18:27:00 GMT permalink Post: 6690486 |
Saw BOAG this weekend
I was in Seattle for a wedding this weekend, and got to see BOAG at the Museum of Flight.
It was gratifying, but I can't say she's in stellar condition. I'd give her a solid "B" grade. For one thing, it drives me nuts that all the literature and display placards all say "the Concorde." I far prefer Concorde to stand on her own. Her paint was dull and oxidized, and the exhibit sort of stands alone, without much in the way of history or surrounding material. It pained me a bit to see her outside in the Seattle weather, too. The interior is nice, being cordoned off by plexiglass that could stand a replacement sometime soon. I didn't see peeling paint. That said, it was a spectacularly more enjoyable experience than the last time I saw Concorde F-BVFA at the Udvar Hazy museum in DC, thanks completely to this thread. I noticed things I'd never seen before, and took a much more profound appreciation of things like the curve and droop of the wing leading edge and the complexity of the engine intakes... and I loved seeing the difference in fuel consumption numbers between Concorde and the SR-71 also on display. My wife thinks I'm a genius because I knew why #4 engine was N1 limited below 60kt and what the little 3/4 tag to the left of the engine EGT gauges was for. Thanks again to all the knowledgeable individuals on this thread. Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
DozyWannabe
September 09, 2011, 18:45:00 GMT permalink Post: 6690514 |
Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
pattern_is_full
July 16, 2016, 16:01:00 GMT permalink Post: 9441981 |
According to this, 5500-6000 feet/1700 meters
Heritage Concorde IIRC from one of the previous posts here, the strong differential required also defined the normal descent/deceleration timing and distance. Power could only be reduced to 94% (N1 or N2, I forget which) or there would not be enough "bleed" air available to maintain the cabin altitude at TOD. (although I could have misinterpreted that - it may have had more to do with maintaining the oblique inlet shocks, or hydraulics, or some such.) Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |
EASAPARTACADEMY
June 24, 2022, 23:14:00 GMT permalink Post: 11251293 |
Point taken GF, but it was discovered during development flying that that the Olympus 593 could be relit, given sufficient IAS, at almost any altitude within the normal flight envelope. The variable inlet would even be automatically scheduled, as a funcion of N1, in order to improve relight performance at lower Mach numbers. I certainly agree that you would decelerate and lose altitude fairly quickly under these conditions, however a multiple flame out was never experienced during the entire 34 years of Concorde flight testing and airline operation. There was, as a matter of interest an un-commanded deployment of a Concorde RAT AT MACH 2!! (The first indications of the event were when the cabin crew complained about 'a loud propeller sound under the rear cabin floor'. A quick scan of the F/E's panel revealed the truth of the matter). The aircraft landed at JFK without incident, and the RAT itself, apart from a very small leak on one of the hydraulic pumps, was more or less un-phased by the event. Although it sounds horrific, a prop rotating in a Mach 2 airstream, the IAS it 'felt' would be no more than 530 KTS at any time. The RAT was of course replaced before the aircraft flew back to LHR.
Not quite sure about your reference to the RAT on an F16 being Hydrazine powered; a Ram Air Turbine is just that, using the freely rotatting propellor to power hydraulics, electrics or both. Or do you mean the the F16 has an emergency power unit? Either way, it's fascinating stuff. Yes, I do remember that the Germans used Hydrazine as a fuel during WW2: The father of one of our Concorde pilots was on an air raid to destroy one o the production plants there, this aviation business is such a small world. ![]() What I found interesting is that the AC generators would remain on-line at all; they drop instantaneously at subsonic speeds and the associated N2 rpm. I believe the hydraulics on the 747 will power flight controls down to a pretty low IAS. Four engine flameout is a very unlikely event, unless one runs into a volcanic cloud. Reply to this quoting this original post. You need to be logged in. Not available on closed threads. |